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隧道建设(中英文) ›› 2021, Vol. 41 ›› Issue (S2): 158-164.DOI: 10.3973/j.issn.2096-4498.2021.S2.020

• 研究与探索 • 上一篇    下一篇

泥质粉砂岩地层地铁盾构掘进渣土改良技术研究

冯利坡1, 廖少明2 *, 周德军1   

  1. 1. 金华市轨道交通集团有限公司, 浙江 金华 321000 2. 同济大学土木工程学院, 上海 200092)
  • 出版日期:2021-12-31 发布日期:2022-03-15
  • 作者简介:冯利坡(1982—),男,河北邯郸人,2013年毕业于同济大学,隧道及地下建筑工程专业,博士,高级工程师,现从事地铁工程设计与施工技术管理工作。E-mail: flpa607@163.com。 *通信作者: 廖少明, E-mail: liaosm@126.com。
  • 基金资助:
    金华市科技计划社会发展类重点项目(2019-3-027

Soil Conditioning Techniques for Shield Tunneling in Argillaceous Siltstone Strata

FENG Lipo1, LIAO Shaoming2, *, ZHOU Dejun1   

  1. (1. Jinhua Rail Transit Group Co., Ltd., Jinhua 321000, Zhejiang, China; 2. College of Civil Engineering, Tongji University, Shanghai 200092, China)
  • Online:2021-12-31 Published:2022-03-15

摘要: 土压平衡盾构在泥质粉砂岩地层中掘进时,因基岩裂隙水发育程度差异性大,易出现螺旋输送机喷涌、渣土流塑性状态差等问题,为确保顺利施工,须进行渣土改良。依托金华—义乌—东阳市域轨道交通金华站—双溪西路站盾构区间工程,室内模拟正常涌水和大量涌水2种工况的渣土状态,添加不同改良剂并开展坍落度试验,研究改良渣土的流塑性。结果表明: 1)为达到渣土坍落度1020 cm的理想改良要求,正常涌水段加水量占土体积比为40%46.3%,此时渣土含水率为27.8%30.6%,与坍落度线性相关; 2)大量涌水段,膨润土或生石灰加入量占土体积比分别为5.5%6.8%5%6.9%。现场验证试验表明,大量涌水段加入相应比例的膨润土或生石灰后,渣土稠度状态得到有效改善,螺旋输送机喷涌问题得以有效控制。

关键词: 土压平衡盾构, 渣土改良, 泥质粉砂岩地层, 坍落度试验

Abstract: When earth pressure balance(EPB) shield tunneling in argillaceous siltstone strata, muck and water gushing of screw conveyor and poor soil plasticity state are often encountered due to the various development degrees of bedrock fissure water. As a result, soil conditioning should be conducted. A laboratory test is conducted on a shield section of Jinhua station to Shuangxi West Road stastion of JinhuaYiwuDongyang urban rail transit under conditions of normal and large amount of water gushing. Various soil conditioning materials are used to carried out slump test to study the plastic fluidity of improved soil. The results show the following: (1) To reach an ideal soil slump of 10~20 cm, the volume ratio of water added to soil is 40%~46.3% in normal water gushing section, and the soil moisture content is 27.8%~30.6%, which is linearly correlated with the slump. (2) In the section with large amount of water gushing, the ratio of bentonite or quicklime to soil volume is 5.5%~6.8% or 5%~6.9%, respectively. The field test results indicate that after adding bentonite or quicklime in the section with large amount of water gushing, the soil consistency can be effectively improved and the mud and water gushing of screw conveyor can be effectively controlled.

Key words: earth pressure balance shield, soil conditioning, argillaceous siltstone strata, slump test

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