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隧道建设(中英文) ›› 2015, Vol. 35 ›› Issue (5): 463-467.DOI: 10.3973/j.issn.1672-741X.2015.05.012

• 施工技术 • 上一篇    下一篇

某运营地铁区间浮置板道床隆起原因分析及整治措施

李丰果1,2, 俞建铂2   

  1. (1. 中铁隧道集团有限公司盾构及掘进技术国家重点实验室, 河南郑州 450001; 2. 中铁隧道集团三处有限公司, 广东深圳 518052)
  • 收稿日期:2014-11-06 修回日期:2015-03-12 出版日期:2015-05-20 发布日期:2015-05-22
  • 作者简介:李丰果(1973—),男,甘肃古浪人,2009年毕业于山东科技大学,建筑与土木工程专业,硕士,教授级高级工程师,主要从事隧道与地下工程施工管理工作。

Case Study on Causes and Countermeasures for Heaving of Slab Track Bed in a Running Metro Tunnel

LI Fengguo1,2, YU Jianbo2   

  1. (1. State Key Laboratory of Shield and Boring Technology, China Railway Tunnel Group Co., Ltd., Zhengzhou 450001, Henan, China; 2. The Third Engineering Co., Ltd., China Railway Tunnel Group, Shenzhen 518052, Guangdong, China)
  • Received:2014-11-06 Revised:2015-03-12 Online:2015-05-20 Published:2015-05-22

摘要:

某已运营近2年的地铁区间浮置板道床出现隆起、下沉情况,针对该类型道床隆起原因及处理方法进行了分析,确认浮置板道床基层与仰拱填充层之间存在空腔,地下水在空腔中形成压力,导致道床发生隆起。为了防止道床面继续发生隆起,采取了钻孔放水降压、注浆填充空腔、将道床及衬砌与基岩锚拉等措施对浮置板道床进行综合治理,达到了预期治理目的。

关键词: 地铁, 浮置板道床, 隆起, 排水, 注浆, 锚拉

Abstract:

Heaving and settlement occur to the track bed of a running Metro tunnel, which has been in service for almost 2 years. In the paper, the causes and countermeasures for the heaving of the track bed are analyzed. It is concluded that there is a gap between the track bed cushion layer and the invert filling layer, the water at the gap results in pressure and causes the track bed heaving. Countermeasures, including water releasing and pressure reducing by means of borehole drilling, gap filling by means of grouting, reinforcing track bed, lining and surrounding rock by means of tie bolting, are taken. In the end, good treatment effect has been achieved.

Key words: Metro, slab track bed, heaving, drainage, grouting, tie bar

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