ISSN 2096-4498

   CN 44-1745/U

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Tunnel Construction ›› 2017, Vol. 37 ›› Issue (7): 864-871.DOI: 10.3973/j.issn.1672-741X.2017.07.013

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Analysis of Causes of Lining Cracking and Ballast Bed Freezing at Railway Tunnel Portal in Cold Regions and Their Countermeasures

ZHENG Bo1, WU Jian1, CHEN Jianping2   

  1. (1. China Railway Southwest Research Institute Co., Ltd., Sichuan 611731, Chengdu, China; 2. China Railway No.8 Engineering Group Co., Ltd., Sichuan 610036, Chengdu, China)
  • Received:2016-11-08 Revised:2017-01-06 Online:2017-07-20 Published:2017-07-26

Abstract:

The causes of lining cracking, waterleakage and ballast bed freezing at portal section of a railway tunnel in Northeast China are analyzed by comprehensive analysis method; and then relevant countermeasures are proposed. The analytical results show that: 1) The cracking of surrounding rock lining is mainly caused by frostheave force of surrounding rock; and it can be effectively avoided by using insulation measure of spraying insulation layer + fireproof mortar and structural reinforcement measure of anchor bolt + crack filling. 2)The water caused ballast bed freezing in tunnel is mainly derived from snow on portal cutting of tunnel and the local waterleakage of inverted arch; and it can be effectively avoided by setting electric heating facilities in ditches on both sides of the tunnel, setting a small dam and horizontal electric heating facilities under the bottom of ballast bed, and setting snowcovered facilities on portal cutting of tunnel and zerofill section of embankment.

Key words: railway tunnel, frostheave force, lining cracking, ballast bed freezing, insulation facility, electric heating facility

CLC Number: